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The Galley Sink Drain 
This page was last updated on 22 March 2003 
During the first two seasons of
use since the restoration, the galley sink continued to plague us with
annoyances.  The original sink I installed, a wonderful, 9" deep
version, was way too deep for the location in the galley--the bottom of the sink
was lower than the waterline outside, so the sink always contained several
inches of water.  On to plan B:  install a shallower (5")
sink.  This worked OK during the first season with the boat, though the
water level was still barely below the bottom of the sink.  When we loaded
the boat heavily the second season with more cruising gear and provisions, water
tended to enter the sink, especially when people were sitting in the
cockpit.  Also, when sailing on port tack if the sink drain was open, water
would come in alarmingly.   
After dealing with this
annoyance, and potential hazard to the safety of the boat, I decided to take the
drastic measure of installing a sump chamber and pump in order to better handle
the sink drain.  Electric pumps tend to be power hungry and prone to
failure, but I didn't see any true choice in this case.  Plus, installing
this rig would allow a seacock to be permanently closed and sealed--always a
good thing. 
  
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       The
        first step was to remove the old drain assembly and hose.  In the
        tight confines of the space beneath the sink, this proved to be fairly
        difficult, and ended up sawing through the metal tailpiece on the sink
        to get that end of the hose free.  Once that was done, I could
        twist it off the seacock tailpiece more easily.  Then, I had to cut
        the drain off the sink too, since the cheap metal tailpiece and its nut
        had corroded together from all that salt water.  Again, the
        relatively tight access (but at least I do have clear access!!) made
        this a bit tougher than it could have been, but I got it done. 
        With
        the old drain out of the way, the first order of business was to seal
        off the now-unnecessary seacock.  I removed the tailpiece and
        replaced it with a bronze plug, and shut the seacock.  Should I
        ever need it again, it will be usable, and I don't intend to remove the
        fitting itself--a blanked-off seacock is as good as no seacock at all,
        especially when the through hull and seacock are only two years old to
        begin with. 
          
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       I
        assembled the various pieces and parts I needed to complete this
        job.  Earlier, I had purchased an Attwood shower sump system, which
        consists of a bilge pump and float switch mounted in a sealed plastic
        container with a variety of hose nipples on one end for intake and
        discharge.  The directions call for the discharge (overboard) hose
        to run continually upwards from the sump to prevent airlock or water
        remaining in the chamber, but should this be impossible, there's a
        provision for drilling a vent hole in the clear plastic cover.  I
        spent quite a bit of time considering my various options for where to
        pump this thing overboard.  The easiest thing would be to install a
        through hull fitting in the topsides just opposite where the pump is
        located, which would end up being a bit aft of amidships on the
        starboard side (where the galley is).  However, I didn't really
        want to install a fitting here, for several reasons.  First and
        foremost, this location would surely lead to an unsightly streak of gunk
        on the side of the hull, a combination of bronze residue, soap scum, and
        food bits from the sink.  Yuck--and totally unacceptable to
        me.  I certainly wouldn't consider locating the discharge anywhere
        but at the gunwale, because nearer the waterline would guarantee that it
        would frequently be below the heeled waterline, and would allow back flooding. 
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        All considerations seemed to point to
        mounting the discharge well aft, probably in the counter where it would
        be out of sight and any residue from the fitting would not be
        particularly visible.  However, mounting the discharge there would
        mean a much longer hose run, and the impossibility of keeping the whole
        line running continually upwards (at least not easily).  And the
        location in the counter could still conceivably allow back siphoning
        into the pump under certain conditions.  On balance, though, this
        seemed to be the best location, so I bought enough hose to r each all
        the way there from the galley.  I also purchased a threaded bronze
        through hull fitting (3/4"), a bronze shutoff valve, and a bronze
        90° tailpiece fitting (all for 3/4" hose).  To complete the
        sump installation, I also purchased some duplex wire and a switch to isolate
        the pump and shut if off if desired.  I had to order a new sink
        drain fitting to replace the one I cut off earlier, since I couldn't
        source one locally. 
         With
        all the pieces on hand, I chose a nice, very warm afternoon (finally!)
        to install the through hull fitting.  After hemming and hawing for
        some time, and looking at the hull in a few places from both inside and
        outside, I chose the location in the starboard counter near the existing
        bilge pump outlet, and, from the inside, drilled a small pilothole to
        the outside.  After confirming the location, I applied some masking
        tape over the hull on the outside to help control chipping; then, still
        outside the hull, I cut a 1" hole with a hole saw (the correct size
        to fit the threaded through hull fitting).  One more hull core
        sample to add to my collection! 
         After
        removing the tape, I tried the fit of the through hull--the hole was a
        bit snug, so I reamed it out a small amount with a drum sander
        attachment on my drill.  Once the fit was right, I cleaned the
        inside of the hole, the hull, and the inside of the hull with some paint
        thinner to remove dust and contaminants. 
        Next, I preassembled the
        bronze shutoff (ball) valve with the 90° bronze tailpiece.  I
        applied some Teflon tape to the threads and tightened the two pieces
        together, ensuring that the nipple faced the way I wanted it to when it
        was tight.  I took the time to do this step ahead of time so that I
        could ensure that the assembly would be properly aligned when I
        installed the valve on the threaded through hull fitting.  Because
        this fitting is above the waterline, I saw no need for a flanged,
        through-bolted seacock, but wanted a solid shutoff valve so that I can
        close this fitting off should there be following seas or other
        conditions that threaten to back siphon into the sump through the
        counter.  For most conditions we expect to experience, this should
        not be an issue. 
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       With
        both sides cleaned up, I heavily gooped up the through hull flange with
        polysulfide caulk, and applied some to the first inch or so of the
        threads as well.  Then, I inserted the fitting into the hull from
        the outside; the fit was tight enough that it stayed by itself while I
        went aboard to install the nut.  On the inside, I applied a bit
        more caulk around the fitting, then screwed the nut down tightly, first
        by hand and then with a wrench.  I inserted a bar into the fitting
        from the inside to hold the mushroom from turning while I tightened the
        nut. 
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       When
        the nut was tight, I cleaned off the excess caulk that squeezed out
        around the nut, and screwed the ball valve assembly onto the remaining
        threads.  The nut below held the through hull tight enough to
        prevent it from turning when I tightened the valve in place.  I did
        twist the whole assembly just enough when it was tight to align the
        valve handle and 90° nipple the correct direction. 
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       Next,
        I went back outside and down to the ground, and cleaned up the caulk
        squeezeout around the mushroom fitting.  
		
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       With
        the fitting all installed and cleaned up and secure, I ran a length of
        3/4" black fabric-reinforced hose from the lazarette to the galley,
        following the path used by the bilge pump hoses.  I secured the end
        of the hose to the new valve and nipple with  an AWAB clamp, and
        routed the hose into the locker beneath the galley where I planned to
        locate the new sump pump.  I let the other end run wild for now,
        and secured the hose with plastic cable ties in several places along its
        run. 
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          I ran a
        length of 14/2
        sheathed safety cable (red and yellow wires) from the positive and
        negative distribution busses behind the electrical panel over to the
        galley.  At the positive distribution end, I installed a 4-amp
        inline fuse, as called for in the pump wiring directions. 
        Following preexisting wiring runs, I threaded the cable along until I
        reached the galley locker where the pump was to be installed, securing
        it every so often with plastic wire ties.  Inside the locker,
        where it would be convenient if needed, I installed a rocker switch to
        allow the power to be shot off to the automatic pump.  It should be
        on most or all of the time, but the switch is a good idea just in case. 
        Next, it was time for the
        final sump installation, wiring, and plumbing connections.  First,
        I secured the plastic top of the sump with six screws, drilling through
        the top into the provided screwholes along the edges.  With the top
        now secured in place, it was time to install the sump chamber in place
        in the locker beneath the sink.  I decided to install it tightly
        against the rear bulkhead, partly because it was the best location, but
        also for the sake of convenience; with access to this locker as
        difficult as it was, and requiring various contortions on my part,
        installing the sump where I did meant that I only needed to install two
        of the four hold down clamps to secure the chamber in place.  Fewer
        fasteners to install whilst standing on one's head is a happy
        thing.  I secured the chamber with two hold down clamps on one
        side, and I drove two longish screws into the rear bulkhead just above
        the top of the sump to effectively hold that side down.  Since I
        had spare clamps, I installed one at the far end just in case the
        chamber showed any inclination to slide athwartships. 
		 With
        the sump now secured in place, I completed the wiring, leaving plenty of
        extra wire bundled up nearby so that I can pull the sump up on top of
        the counter for maintenance without undoing the wiring, should such
        maintenance become necessary.  Finally, I installed the new sink
        drain to replace the one that I was forced to cut earlier in the process, 
        and connected the discharge hose to the appropriate nipple on the
        sump.  The fabric-reinforced hose proved to lack the stiffness
        needed to make the tight bend between the sink drain and the sump
        intake, so I rummaged around in the shop and found a length of
        wire-reinforced hardwall hose left over from something else, and
        installed that from the sink to the sump. 
		Project
        complete.   | 
     
    
      
         
		Update:  2008 
		After dealing with a variety of ultimately unsuitable modifications to 
		the galley sink setup, I decided to completely reconfigure the system, 
		reverting to a deep sink and locating a new sump chamber in the bilge, 
		far removed from the sink itself so as to address several issues with 
		the "third try's a charm" semi-original setup that I installed in 2003.../maintenance/maintenancelog2009.html#71809
		Read more about the newest changes in the
		winter 
		2008 refit log. 
  Update:  July 2009 
		 The sealed automatic switch (non-Mercury, non-float) that came with 
		the Johnson sump chamber failed to work acceptably or even marginally, 
		forcing me to replace it with an older, spare mercury float switch left 
		over from my previous installation.  Read more about the fix
		here. 
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